Loading...
HomeMy WebLinkAbout000-000-0041>/ Juh.19 '96 10:18 KONICA FAX 720 p 2 NINE _GMMM Mnl.rrinl.c 60 • ) Saginrcrink (nhSWI '11@stln/; and Mic), l41 u�► LTA qm chat lnotr (916) (i11K1 "!l1i lkulil'ir.:rtinr :i01•(Ki;:b Inspector's Dally Report OROJECT: Butte County Courthouse Addition FILE NO: 95457 INSPECTOR: J. Sears PAGE NO; 1 of 2 WEATHER: Clear Hot DATE: 07-11-96 Arrived at the job at 1000 hr for torque testing of expansion anchors installed in the top of the concrete stairwell wall adjacent to Grid Line III], between Grid Lines AA and BB. These anchors were inspected earlier (See Inspector's Daily Report dated -04-09-96) and found to be only finger tight Contractor was notified of the deficiency and stated he would correct it_ Inspector Virgil Hancock discovered these bolts had not been tightened prior to covering with sheetrock and required the sheet rock be removed A torque wrench was used to tighten the anchors to 175 ft -lb. Both expansion anchors at this location are now tightened to 175 ft -lb of torque. Contractor was preparing to place concrete for the Sallyport columns and had completed excavation for the bases. The columns for this structure (TS 6 x 6) are to be encased in concrete, without baseplates and anchor bolts. Contractor has elected to over -excavate the column footings to provide a concrete base upon which to seat the column. At this time, contractor is preparing to place concrete for the bases. Rebar cages which surround the column have been lengthened to extend into the deepened base. Although the cages were found to be somewhat rusty, they were judged to be satisfactory. Excavations were inspected and found to be firm and free of loose soil Two of the columns are aligned over a 10" water line anda special detail was prepared by the engineer to shift the column loads to the sides of the water pipe This detail required Ju1.19 '96 10:19 KONICA FAX 720 P. 3 it re as jun.' -611-d ■o► , a '�l DIK.Ak.ab. e Da PROJECT: Butte County Courthouse Addition, Concrete FILE NO: 95457 INSPECTOR: J. Sears PAGE NO: Z Of 2 Meltr;nle Nou i;npinenrhul 04h"*a t Iir A;1 Testing nml Chirn. CA lnrpectim 10420 _ I.kAll1 1.1116) 0trtifiencien 901-M26 WEATHER: Clear, Hot DATE: 07-11-96 encasing the water pipe with an insulation -packed sleeve and installing a rebar cage on each side of the pipe. A grade beam is to be constructed to span over the pipe and be supported by the rebar cages. Initial concrete placement in this assembly is to be to the level of the bottom of the column. All preparations for placement of concrete over the water pipe (both locations) was as shown in the special detail. Departed the job at 1130 hr. due to other work commitments. ATC employee, Brad Forsythe will arrive at 1200 hr. for special insoection of CAncrAtp nlaramont fnr thn nnlvmn hnann